Articles
The M1 Garand
This gun has been relegated to second class status by most of
the shooters and all because very few gunsmiths knew how to make
them shoot below 1 MOA. I found out later than even the gunsmiths
who built some guns which shot under 1 MOA also built a bunch
of guns that would not shoot that well. I'm sure they were puzzled
as to why, some of the guns, which didn't shoot well, had custom
barrels on them and still the accuracy was less than desired.
After spending 10 years building double lugged M-14/M1A's practically
all of which shot 1 MOA or less, I decided to take another look
at the M-1 to see if the things which worked well on that gun
also would work on the M-1. The first innovation was to put a
lug on the rear of the receiver so it could be bolted down. Without
a doubt this was successful. It relieved the trigger guard of
its job of holding the gun together and greatly enhanced the life
of the bedding job. Later, I added the front lugs to finish the
job. There are two front lugs both small and mounted on the right
and left sides of the receiver just under the front corners of
the trigger plate. The action is pillar bedded with great care.
Custom barrels were installed, op-rods aligned properly, and gas
cylinders were also fitted properly. I expected dramatic results
when I tested the first one but I was disappointed. Many of the
guns did shoot under 1 MOA, but many did not which was very frustrating.
The problem went into my hair-top computer and weeks later the
analysis came out. The gun actually had two problems, both of
which must be addressed in order to obtain peak accuracy and also
to retain it. The first was that long skinny op-rod. I knew how
to straighten and align them but I didn't know how to prevent
them from bending later. Accuracy procedures up to then said that
the op-rod should touch nothing in its cycle so metal was cleared
away in the stock ferrule, the liners were removed from the hand
guard all in an effort to give the op-rod unfettered room to move
but also unfettered room to bend. Clearly we needed some op-guide
system like the M-14 has but how to put one on a rod with two
bends in it? Further work for the hair-top computer. The solution
came one day when I was examining a DCM issue M-1 and noticed
a .050 gap between the bottom of the op-rod and the ferrule. Why
the gap? Well Dummy, it's a combat gun and you need such gaps
so the gun will function even if cruded up with mud or sand and
stuff like that. Hmm. None of my shooters use these M-1's as combat
guns so why do I
need poorly fitted parts? I wonder what would happen if we went
in just the opposite direction? Instead of loose fitting combat
parts we have snug fitting match parts, but again, how to do it
on an op-rod with two bends in it. Then came the solution. The
guide system had to be two pieces. The forward piece a circular
track epoxyed in the upper hand guard and a lower track silver
soldered in the stock ferrule. Both had to be fitted just right.
They could not bind the op-rod, but they had to almost touch it,
a light slide fit. I built the first pair and installed it in
my own M-1 hoping it would still function without binding. I loaded
a clip of Israeli ball and shot it into a rotten tree stump in
my yard. It worked and thus a serious durability problem on the
M-1 was solved. That still left the second problem.
I became aware of it after building a rear lugged M-1 with a
Krieger barrel for a customer in Washington State. On the test
bench it shot 2¼ inches. For a Krieger barrel this was
not acceptable so I set the gun aside with a feeling of frustration.
I knew the gun had been built with care. I knew the barrel was
first class. It had to be something else. A week later the hair-top
computer spun out the answer. It was timing. The bullet was still
caught in the rifling when the op-rod started to move rearward.
It set up barrel vibrations, which affected accuracy. This explained
all those guns with good components, which did not shoot well.
They could all have been made to shoot good if a way had been
found to delay the op-rod function until the bullet just cleared
the muzzle. The problem dictated the solution. When the bullet
cleared the gas port a high-pressure impulse of gas filled the
chamber between the plug and piston tip. If the volume of this
space was just right the gun shot good, if not, it shot poorly.
Perhaps we could do something to make the volume variable. The
solution was an adjustable gas plug. A plug with a threaded bore
with two setscrews mounted inside. By adjusting them outward the
volume was increased. More volume, more time needed to fill it.
Time measured in parts of a millisecond. To say this solution
worked is an understatement. It was the missing link, the last
rear hurdle. Back to that gun for Washington State. I pulled the
plug on it took dimensions off it and made a crude drawing. On
my lathe I made my first one that afternoon. Next morning, out
to the test bench, first group 2¼ inch, which is what I
expected. First adjustment, outward ½ turn, group shrunk
to 2 in. On the fifth ½ turn adjustment; the group was
.800 in. I sent all five groups to my customer and explained what
I had done. To this day, I've never heard a word from him but
then,
us gunsmiths rarely ever hear from customers unless something
is wrong, so I wasn't surprised. I've learned no news is good
news.
With these innovations the average accuracy levels came below
1 MOA. It was only an occasional gun, which didn't make it, and
this was usually traceable to poor barrels. Recent work with fire
lapping has made some GI barrels and Douglas barrels shoot like
Kreiger barrels. I'm really pleased with this as it cuts barrel
cost dramatically. All this caused my reputation on the M-1 to
soar to such a point that a military armorer said "If you
want a good shooting M-1 get Clint Fowler to build it." Getting
such praise from a military armorer is rare. Those guys are convinced
that service rifles are their art form for a civilian gunsmith
to be recognized is rare.
The most cost effective gun I build is a DCM M-1 with new GI
barrel, a rear lug and pillar bedding, with op-rod tracks and
adj. Gas plug and maybe fire lapping. It can be expected to shoot
1 inch or less at 100 yards with good ammo. All provided at a
total cost under $500.00.
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